Evening all,
Qualified last, not too surprising considering the bike hadn't ever turned a wheel and I was checking it out (not to mention the rider also getting his head around being on track after 30+ years). Then put a hole through the right hand piston after 4 laps of race 1. Up until that point the bike seemed to be going fine, much faster than the rider certainly. The Seeley chassis was a delight, the Maxton forks giving some chatter under braking (which never rose to full-on stopping, some work to do on set-up). I did at least drop 14 seconds on Qualifying time before the engine said "sod this" so progress made in a small respect.
So, things to do:
1. Lose 4 st. in weight and get in some exercise (cheap to do)
2. Get in a bunch of practice (££££)
3. Re-build the engine (I think a crank seal went because the LH plug colour seemed OK so not drastically under jetted) (£££££££)
Had a great weekend apart from my race performance, but with application I may rise to a midfield runner, even at my decrepit age. The bike and build gathered some appreciative interest and went through scrutineering with out comment which personally was very pleasing.
You can certainly have a go SD, got to be faster than I was this weekend
Team Zunspec Race HQ Snetterton 2013
